Pilot won't stay lit - Vermont Castings Radiance 2560

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scatr

New Member
Dec 22, 2011
5
Southwest CT
I have a 16 year old Vermont Castings gas log stove and I can't get the pilot to stay lit. I can get the piezo to fire and the flame to catch. But if I let go of that gas knob, no matter how long I hold it down, the flame will go out. I replaced the thermocouple in case that was it, but it didn't help. I have also adjusted the screw that is supposed to adjust the size of the pilot flame, but it doesn't seem to make any difference. I can tell that the flame is too small. It does not reach all the way to the thermopile or the thermocouple. I have tried to blow out the pilot hood with compressed air and have tried to get a small wire down there (but it's really hard to get in there) just in case there is any blockage. So far, no luck.

Every year this thing has been a bear to get lit but this year I can't get it going at all.

Any other recommendations, or is it time to call in a pro? Thanks for your help
 
If the pilot can't reach the Thermocouple (T-C), you will not get the pilot to hold.
If you can't turn the pilot up, you may have a gas pressure issue.
Are all of the gas shut-offs completely wide open - ie. IN-LINE with
the gas flow? Are you running NG or LP?
Do you still have the T-C you pulled out? If you do, you can test it
with a flame -match, lighter, candle - & a multimeter to see if it was
indeed bad. Another check might be to make sure the new one is
correctly seated in the valve body, but you HAVE to get the top 3/8"
of the T-C engulfed the the pilot flame...
 
Trying this again .... posted a reply but it disappeared...

Sounds like it could be a pressure issue I guess but not sure what would have changed to cause it. It's liquid propane, 3 100 gallon tanks ganged together to make 1 virtual 300 gallon tank. The gas line run to the VC is about 25 feet at most.

I do have the old thermocouple. I get putting a flame to it and I do have a multimeter, but how should I use it to test the thermocouple?
 
scatr said:
Trying this again .... posted a reply but it disappeared...

Sounds like it could be a pressure issue I guess but not sure what would have changed to cause it. It's liquid propane, 3 100 gallon tanks ganged together to make 1 virtual 300 gallon tank. The gas line run to the VC is about 25 feet at most.

Not sure how cold it is where you're at, but LP can be affected by temperature...

I do have the old thermocouple. I get putting a flame to it and I do have a multimeter, but how should I use it to test the thermocouple?

This is best done with 2 people unless you have alligator clips on your probes, but basically,
put the flame to the top 3/8" of the T-C. Put one probe on the extreme end (the small silver
colored disc that actually goes into the valve) of the T-C & the other on the copper shell of
the T-C lead... see if you get over 27 mV...
 
I checked the old T-C with my multi-meter. I don't know how to use this thing well enough to be completely sure of my results though. I *think* what I got was no reading at all on AC voltage, no matter where I put the dial. On DC voltage, I did get readings, and best I can tell it would settle in around 18. It would jump wildly all over the place but if it settled in it was around 18. So maybe it's reading 18 mV?

Anyway, seems like it's possible there's a pressure issue so I'm going to get the gas company in to take a look and see about getting it going. Thanks for all your help and Merry Christmas.
 
If you got 18 mV on the DC scale, it's not strong enough to hold a pilot.
You may wanna duplicate the test on your new T-C. It's not unheard of
to get a bad one right from the manufacturer...
We're here to help, no thanks needed...
Good luck & Merry Christmas back atcha!
 
Just to tell you the end of the story... had the gas company out, and the gas pressure was fine. The thing where the gas comes out (technical term) needed to be cleaned. Now I know, for the next time. I did the compressed air thing, but it needed to be taken out and physically cleaned out. Working great now.
 
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